Obi-Wan's Tow Rig
During the summer of '99, I started looking around for stouter axles
to put under my
newly-lifted '95 YJ. Front Dana 44's from a narrow-track '80+
Jeep (Grand) Wagoneer are popular swaps, so when I heard a friend had
an '83 with a dead engine, I nearly bought it. At the same time, I
noticed another '83 with a good engine and dead tranny for sale cheap
in the paper. The gears in my head started turning, and I figured I
could combine the two to get a good tow rig and beefy axles for the
sum of $600. That deal fell through, but it got me thinking about
having a tow rig. With our first baby expected to arrive just three
months before the 2000 Moab Easter Jeep Safari, we got to thinking
that we really didn't want to drive 13 hours with a baby in my
trail-built YJ. We both
liked the idea of an SJ (full size Cherokee/Wagoneer/Grand Wagoneer)
for use both around town and on the highway, so we began looking for
a suitable model.
The first place I started gathering info was the
IFSJA web site.
Then I started hanging out on the
FSJ-List mailing list.
Both are excellent sources of info on these
classic beasts. Since our main reason for getting an SJ was to tow,
I kept my eye out for something with a 401 V8 and good gearing. Around
Lincoln, those are very rare birds. After looking for over a month, we
found our truck in the Thrifty
Nickel. 401 V8, 3.54 gears, very little rust, decent interior.
It wasn't pretty and needed a few things fixed right away, but overall,
it was just what we were looking for. I was the first of 20-some
people to call about it on the first day, and we brought it home
Friday, 29 Oct 1999.
I had to promise not to touch it until after I finished remodelling
our first baby's bedroom, so it mostly just took up space in our
driveway initially. The Moab trip fell through, fortunately. 2.5
years later, I still haven't been back, and the Wag is still a work
in progress. I tore the engine out of it in June 2000 to fix the
low oil pressure, and didn't get it back in until August 2002, so
it just took up space in my garage for over two years. Now that it's
back on the road and I'm nearly done remodelling our second baby's
bedroom, I've got lots of little things to fix on it before my wife
can start driving it frequently. It will eventually be her daily
driver, since our family of four is already cozy in her Honda Accord,
and a very tight fit in my Wrangler.
I've half-affectionately been calling this thing a basket case.
Here's a list of the things that were broken or otherwise needed
attention, and what I did to fix them. These all existed when I
bought the rig; I have yet to cause any new problems myself.
- A/C didn't work. I knew this when I bought it. This could
have been the biggest expense, and is definitely not optional
for us on long road trips. At least we had a few months before
we'd need it. After spending a little quality time with my
multimeter underneath the dash in June 2000, this turned out to
be just an unplugged wire and a corroded blower fan switch that
needed cleaning. Blows ice cold now.
- Electric motor that raises the rear
window didn't work. The switch had even been removed
from the dash, but I got a replacement from a friend who was
parting out a similar truck. This is a common malady for these
rigs. The motor had been removed from the tailgate, and all the
wiring had been snipped. Replaced the motor & all the wiring,
readjusted the safety switch that prevents raising the window
with the tailgate open, and now all is well.
- Exhaust was missing behind the muffler, and what remained
was pretty beat up. With the windows down, the fumes were pretty
bad. This was replaced in January with a
custom 2.5" exhaust from Exhaust Pros.
I also tightened a few exhaust manifold bolts to eliminate the
last of the exhaust leaks. 2.5 years later, some of them have
returned.
- The first time we gassed it up, we found a bad gas leak right
at the mouth of the filler tube. Unless you held the nozzle
just right, gas would pour down the inside of the outer
body panel and onto the ground behind the rear tire. I had
to replace the filler hose.
- Old 2-post AM/FM/Cassette radio didn't work. Turned out the
wires were all snipped at the door hinges by a DSPO, and the
radio was missing the speaker wire adapter. A couple of the
original speakers failed an ohmmeter test anyway, so they're
shot. I installed a new DIN-sized CD
player and speakers to replace them.
- Cardboard glove box is falling apart. Plastic replacmenets
are $25; cardboard ones from the dealer are $12. At least removing
it makes replacing the radio wires easier. Got a new one from the
dealer, but am waiting til after the new stereo's in to install it.
- The suspension felt kind of squishy, as though the shocks were
starting to die. Replaced them with
Rancho RSX's.
- The inner support for the center arm rest for the front seats was
broken. Had to remove the cover and padding and weld it back
together with some angle iron for additional support.
- The right shoulder of the driver seat started leaning back the more
I drove it. I took the wrong approach to
repairing it, but got it done.
- The negative battery cable connector fit pretty loose even when
completely tightened. Needed a new one. The battery wasn't
secured to the tray, either. A bungee cord fixes that for now.
- TH400 auto tranny seemed good at first, but after a few months,
went belly up and needed a complete rebuild for $1000. The root
of the problem was a clogged filter that burned up the pump.
At least now I know I have a like-new tranny that shouldn't
ever trouble me again.
- The starting system developed problems the spring of 2000.
It would start fine when cold, but if you tried to start it hot,
it would crank twice & then the battery would die. This was the
result of three problems combined. The starter/solenoid cable
was shot, the starter needed replacment with a rebuilt unit, and
the battery needed replacement with an Optima red-top.
- The engine oil pressure was low. Very low -- 5 psi at warm
idle. A mechanical gauge in the engine bay verified these numbers.
I wish I'd noticed this before I bought the truck, or even before
I had the tranny rebuilt. An oil pump rebuild didn't help.
While checking on the main and rod bearing clearance, I opened
a whole pandora's box of engine problems. The end result was
that it sat in my garage for two years while I
rebuilt the engine myself (it actually only
took a few months to rebuild it; the rest of the time I got
sidetracked).
- Both front wheel bearings were shot. The driver side bearing
was noisy enough that I could hear it while driving. Upon further
investigation, I realized the passenger side was nearly as bad.
- The steering shaft U-joint practically crumbled in my hand
when I removed it to paint the engine bay during the engine
rebuild. Replaced it with a Spicer 5-103X U-joint.
- Discovered a pin-hole leak in the rear side of the top part of the
radiator after the rebuild. I'm gonna see if some of
that stop-leak liquid fixes it. Stupid me didn't have the
radiator checked while it was out of the vehicle.
- Immediately after the engine rebuild (during the cam breakin), my
corroded ammeter connections let all the magic smoke out
from under the dash. I was able to turn off the engine before
flames appeared, then bypassed the ammeter by snipping the yellow
wire that runs from the starter solenoid to the dash and re-routing
it to the positive terminal on the alternator. The red wire that
originally ran from the alternator to the dash board stayed in
place to provide power to the instrument cluster, ignition switch,
etc. The ammeter is now inoperable, but at least I don't have
all the current from the alternator passing through the dash and
back out again en route to the battery. While I had the instrument
cluster out, I replaced a handful of burnt out gauge lights and
secured one of the plastic faces that had always been loose.
- Cruise control doesn't work. Haven't looked into why. I might
be missing a control box.
- Headliner is gone. The remaining backing is the same color as
the rest of the interior, so it really doesn't look bad as is.
Someday I'll put a new one in.
- Horn doesn't work. As with the radio, the wire inside the
steering column was snipped by a DSPO. Gotta pull the entire
wheel to replace it.
- Speaking of the steering wheel, the center insert that holds
the horn "button" is held on loosly by two wood screws rather
than the threaded machine screws that it came with. Not sure
if the thread holes are repairable, so I may grab another one
from a junk yard.
- The lower seals (called "wipes") on all the openable windows
were shot and in need of replacement.
Funny how rubber does that after 25 years in the sun.
- The body is structurally sound, but ... well ... ugly. It's
dark brown with a badly-cracked 4" tall woodgrain decal running
the length of it. The paint is showing its age. The rocker
panels are badly rusted, and there are some spots missing from
between the grille & front bumper. The left rear quarter panel
is also wrinkled. I got some replacement body panels in a trade
with a friend, and another local friend went to school for auto
body work, so I've got the resources to fix this some day.
- The full-time 4WD BW1339 Quadra-Trac has a Mile Marker part-time
conversion kit on it. I haven't checked yet to see if it has
the 16% overdrive, but I think it does. While the part-time kit
gives better gas mileage in 2WD, I'd really prefer the original
full-time operation, which would require swapping the existing
t-case and manual hubs with stockers. The same friend mentioned
above gave me an un-molested Quadra-Trac with only 36,000 original
miles on it, so I can switch that over some day, too.
- The heater box was clogged with leaves
and crud which prevented much air flow. I dismantled it to clean it
out, installed a screen to preven it from happening again, and
replaced my leaky radiator while I was at it.
- One thermostat housing bolt had an object in it that prevented
the bolt from gripping well, and it leaked slightly. Trying to fix it
snowballed into installing a new Edelbrock
Performer intake manifold.
- My original steering stabilizer was shot, so I decided to go
all out and replaced it with with a
Trailmaster 4-Way coil-over stabilizer.
The problem turned out to be a bad ball joint, but the stabilizer
doesn't hurt.
- The gas mileage wasn't great
after the engine rebuild, but I'm working on improving it.
- The gas gauge never registered "full" and there were gas fumes in
the cabin during long trips, so I dropped
the gas tank to fix these problems.
- In an effort to improve gas mileage, power, and idle quality, I
upgraded the ignition with
an MSD 6T and Motorcraft distributor.
High-priority list of things to fix first:
- Inspect rear brakes
- Track down rough idle (valves? exhaust?)
Here's the short list
of a bunch of the miscellaneous parts I'm looking for. If anyone's
parting out a '70's Wagoneer or Cherokee and wants to get rid of some
of these parts, please let me know. In November 2002, I bought a
'78 Wagoneer from a junk yard that I'm now
parting out. In August 2003, I bought an '87
Grand Wagoneer that I'm also parting out.
The FSJ Invasion in Ouray, CO,
(15-17 Aug 2002) was a blast. 94 vehicles showed up to celebrate the
40th anniversary of the introduction of the full-size Jeep.
Visit the Nebraska FSJ List
Back to Obi-Wan's Jeep page
last updated 26 Jul 2005
Obi-Wan (obiwan@jedi.com)
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