Premier Power Welder
Once I started making custom upgrades to my Jeep, it quickly became
apparent that either I'd spend many paychecks paying professional
welders to do my work for me, or I needed to learn how to weld myself.
I opted for the latter, obviously, and signed up for a $55, 10-Saturday
class on MIG welding at the local
community college.
For those considering this, MIG welding is trivial. The hard part
is getting the voltage & wire speed set right, but once done, a monkey
can run the welding gun. I had planned on getting a 110-volt MIG
welder before I began my serious upgrades this summer. They generally
run about $500-700 for models with 20-50% duty cycles and true gas
(MIG/GMAW) capability which can weld metal up to 1/4" thick.
Then, while I was out in Moab
wandering around the vendor displays, I got sucked into the
Premier Power Welder
booth. They were having a sale that saved me $200, bringing the price
for their on-board stick welder with a 160-amp alternator down to US$699.
That's not much more than I'd have paid for a MIG welder, and the Premier
would be portable. When Pat Gremillion taught me to stick weld on his
personal unit (his famous orange Bronco, Der Welder Wagon, was setup
next to the booth), I decided it wasn't that much tougher than MIG, and
bought one. Besides, they said it could be converted to a MIG welder
by simply purchasing a normal wire feeder from my local welding supply
outlet.
Unfortunately, that's when the headaches began. We all got home from
Moab early the next week, and I received my new welder a week after
that. I opened it up to find they'd shipped me an alternator with a
single V pulley instead of the serpentine required by my '95 YJ. So
much for installing it that weekend. I called Premier, and they
apologized and exchanged the pulley in a few days. Turns out Jan had
written down the wrong pulley type when she took my order in Moab.
While waiting for the new pulley, I shopped around town and bought
the other welding tools I'd need. It turns out that the wire feeder
required to convert the Premier to MIG costs $600-900 -- more than
the cost of an entire home MIG welder. The resulting setup would
have basically been a commercial-quality welder, but that's overkill
for me.
Busy evenings kept me from installing it for a week. When I did try
to install it, I removed my York air compressor,
which sits over the alternator, then removed my old 90-amp alternator.
When I tried to install the new 160-amp alternator, I found that the
mounting brackets didn't even come close to matching up. Grrr. So
much for installing it before the
4x4 Fest that weekend.
When I called Premier the next day, I found that Pat & Jan were out
of town. I dealt with Becky (their daughter), who was exceptionally
nice and apologetic, but not terribly knowledgeable about the details
of the various alternators they offered. I faxxed her a drawing of
the mounting brackets on my stock alternator, while she tried to get
a hold of Pat on their trip. After several days, they thought
that what I needed was a 170-amp Chrysler-face alternator. Unfortunately,
they were back ordered, and weren't expected in until late that week,
which was also when Pat & Jan were due back. I sent back my 160-amp
since that obviously wouldn't work. By the next Monday, I hadn't
heard anything, so I called to see what was up. Jan confirmed that
I did indeed need the 170-amp Chrysler face, and that she apparently
completely overlooked what type of vehicle I had when she took my order.
The bad news was that the 170-amp was $100 more than the 160-amp,
bringing my total to $800. That was pushing my price limit for a
stick welder (now $200-300 more than the MIG welder I would have
gotten originally), but I agreed, and Jan said I should receive the
new alternator late that week.
When the new alternator arrived, other priorities kept me from
installing it for a while. I finally took the time to hook it up
the night before I was to take some friends wheeling for the day.
I got everything hooked up, but chickened out when it came time
to throw the switch at midnight Saturday, just hours before we
were to leave. I let it sit for another 10 days until A) I wasn't
about to leave town, B) it wasn't raining (no lights in the garage),
and C) family had left town after my brother's wedding.
It's a good thing, too, because when I finally did hook everything
up and start the engine, I got no juice from the alternator. I
measured the voltage on the four regulator wires at the three engine
states (just like the manual says), and called Pat at Premier.
He gave me several things to check, none of which worked. He called
his alternator manufacturer the next morning, and they decided that
the stator was bad in my alternator, so they sent me a new one.
It arrived the next Tuesday, after I'd been without a running Jeep
for six days. I installed the alternator in about 20 minutes (I'm
getting good at that by now), and fired it up. It appeared to do
its job, but it whined like you wouldn't believe -- so loud, in fact,
that my wife could hear it over the engine noise while following
a block behind me in a different car. The previous Premier
alternator didn't do that, so I think there's still a problem.
Then again, that could be because the previous alternator wasn't
charging. Whining Premier alternators are apparently not rare, but
mine was excessive. Some of the voltages at the regulator are
different from what Premier specifies, which worried me. I called
Pat again (he remembers me now). He said the voltages were correct,
which must mean the docs are wrong, but he was baffled as to the
cause of the noise. They're sending me a fourth alternator
Thursday morning, which means I'll be without the Jeep until Monday.
I hate driving my wife's car in town, and our untimely rural house
sitting stint keeps me out of biking range.
The latest arrival from my alternator-of-the-week-club came Monday
morning. The shaft doesn't seem like it spins (by hand) any smoother
than that of the noisy unit, but that didn't appear to be the problem.
I installed it Tuesday night, and it works great. No noise whatsoever.
Looks like the job is finally complete.
Nearly two months after I paid for the thing at Moab, that's where I
currently (10 Jun 98) stand. My advice to the rest of you is to know
exactly what you'll need before sending in your order. Pre-1990 Jeeps
(and other Chrysler vehicles) can use the 160-amp alternator. Post-1990
Jeeps (& family) need the 170-amp Chrysler face alternator. 1990 owners
need to look under the hood to see which style they've got. YJ's late
in the '95 production run may actually have a TJ engine, and therefore
may need the TJ installation instructions.
At this point, I'd recommend that your first welder be a simple, 115-V
garage unit (preferably gas-capable MIG for beginners). If you find
that you need an on-board welder, you can get one later.
Installation (finally)
I've rambled long enough about the ordeal I went through to get the
thing to my door. Here's how to install it.
The toughest part of the installation is figuring out where to put
the control box, which is roughly 4x4x8", plus all the wires and the
regulator. Premier recommends that you place the control box on the
opposite side of the vehicle from the battery, and insists that
you keep it at least 12" from the battery. Placing it where the factory
jack used to sit is therefore acceptable, but not recommended. I didn't
want to get rid of my jack anyway, so I squeezed the control box onto
the driver's side fender well just outboard of the air filter box. My
cruise control unit already sits there, so it was a tight fit. Not only
is this location easy to access, it's also pretty well protected from
water and mud that may fly up into my engine compartment.
The first order of business was to fabricate some mounts for the box
and regulator, since the fenderwell isn't flat. I got a 1/8"x1.25"
strip of steel with holes in it. I cut a couple 3-4" long strips
and bent them into V's. One side of each V was bolted to the bottom
of the control box, while the other side was bolted to the fender well.
When positioning the control box, make very sure that it sits
flat and isn't twisted slightly. Several things inside the box
(including the big heat sink) cannot touch the sides of the box without
causing problems.
I removed the regulator from the side of the box and moved it to the
end. I made another bracket from the same strip metal that extended
the regulator horizontally straight out from the top of the control
box, positioning it right above my cruise control unit (like I said,
space here was tight).
I already had a hand throttle installed
before I got the welder, so I didn't install the one Premier sent.
You're on your own for placement and routing if you use theirs.
Before you do anything with the alternator or related wiring, be
sure to first remove the cable from the negative battery
terminal! There's a lot of juice running through those
cables, and you don't want it to take any short cuts, especially
through you.
Next, remove the factory alternator. If you've got my
York air compressor setup, you'll have to remove the compressor first
so you can get to the alternator. On my '95 YJ 2.5L, there were
two bolts with 15mm heads. The one below the alternator is threaded
into the mount and has no nut. The one above is longer and has a nut
behind the mount. The upper bolt is long enough (4.5"?) to pass through
the front alternator ear, the mounting bracket, and the bushing in the
back ear. In order to avoid removing the bushing from the back ear,
I picked up a 3.5" 3/8" bolt with two washers and a nylock nut to
replace the OEM upper bolt. This will make it much easier to swap the
old alternator back in place in an emergency.
Once the old alternator is free, point it face down and disconnect the
wiring harness. Five nuts hold the wiring harness to the alternator
using 7mm and 10mm nuts.
Along with the new alternator, Premier sent
a 50-ohm resistor that's to be mounted between the two 7mm wiring harness
leads. The brown ignition wire from the PPW control box should also be
mounted to the 7mm lead farthest from the 10mm ground lead. This will
get you the much-sought-after keyed ignition voltage. After making these
connections, make sure you tape off all five of the old harness leads
to avoid any unwanted electrical connections. Once everything is
working, you can warm up the heat shrink tubing to protect the harness.
There are two wires coming from the control box that want to be
connected to the positive battery terminal. The best place that I
could find to do this was where the positive battery wire is bolted
into the Power Distribution Center, aka the engine compartment fuse
box. Unfortunately, this is about as far away from where I mounted
the control box as you can possibly get. I solved the problem by
buying an 18" 4awg starter cable for $5 to use as an extension.
Make sure that you insulate the connection between the control box
wires and the extension using plenty of electrical tape or heat
shrink tubing. If that connection ever touches grounded metal,
you'll see fireworks.
The rest of the connections from the control box are pretty self
explanatory. All the wires are very well labeled, and their
corresponding connection points on the back of the alternator are
pretty obvious.
Once you've got everything plugged in, put your alternator belt
back on and start up the engine. Don't forget to reconnect the
negative battery cable first -- it won't start if you don't (oops).
Get a volt meter and verify that the alternator is working by testing
the voltage between each of the four regulator wires and ground.
The installation instructions provided by Premier document what each
of these voltages should be under various conditions. If your
numbers aren't close to what they specify, you've got a problem.
On my setup ('95 YJ), the second test (key on, engine off) had
identical results to the first test (all off), which differed from
what the instructions dictated. Pat said that was OK. This is
probably because I wired the brown ignition wire to an old OEM
alternator lead, which isn't hot until the engine starts.
If the above numbers work out, it's time to give it a real world
test (read: play with it). If your vehicle has a voltage gauge,
verify that the needle's where it should be (around 14 V). My
'95 YJ dropped from 14.7 with the OEM alternator to 14.2 with the
Premier alternator, but that's still well within the acceptable
range.
Next, try out the electrical outlet. Find an incandescent light or
a power tool and plug it in. Turn on the master and power tool
switches on the Premier's control box, then raise the engine RPM
until the voltage gauge reads 115V. Turn on your appliance and
see what happens. If nothing burns up, go somewhere... anywhere...
and try welding a couple beads on some 3/16" or thicker metal. If
that works, declare the unit to be functional.
One thing to keep in mind is that whenever the control unit's
master switch is on, which is whenever you're using it for fun stuff,
there is no charge going to your battery. Whenever you're not using
the Premier for a length of time, you should turn off the master
switch so your battery doesn't run dead from powering the engine
with no help from the alternator.
Overall Impressions
After a bit of practice on a sheet of 3/16" steel, I was able to
get some decent looking welds. The high frequency current (used
by the Premier instead of high amperage) makes the arc whistle when
you weld, which would make the dwarves proud. I was able to fix a
friend's broken seat bracket, made of 1/8" (or thinner) steel.
That's about the minimum you can weld with the Premier. I tried
running beads on some 16 gauge (or so) steel, and couldn't get a decent
bead without burning clear through. Since a lot of my future welding
will likely be on thinner metal like that, I'm wondering if I might
have been better off just getting a good MIG welder instead of the
Premier. If you've got the cash, get one of each. Sears advertises a
Craftsman MIG welder (gas-ready) for $300. That plus the Premier
should cover just about any thickness or type of metal you're likely
to come across.
One good book for beginning welders is the
Welder's Handbook by Richard Finch. If you're just getting started,
this book will bring you up to speed on the various popular types of
welding.
Confused about the thickness of a particular gauge of wire or
sheet metal? This chart lists the
thickness and weight for each gauge in both English and metric
units.
Toubleshooting
I've had a couple problems with my Premier alternator since I installed
it. In order to save you some trouble and take some load off Pat,
I'll list the problems and solutions here.
- Problem: Alternator stopped charging battery. Voltage
gauge on dash dropped steadily to 12 V. Check engine light
came on and gave some electrically-related DTC
that I now forget. The stator light (red/orange) on the Premier
voltage regulator was out, and the blue wire (stator voltage)
read 0 volts, which indicated that the alternator wasn't engaged
and sending a charge to the battery. Under normal circumstances,
the blue wire should show a varying voltage that gets higher as
the battery needs more juice.
Solution: The alternator and the mess of wires connected
to it (which should have been sealed in shrink-wrap tubing)
had gotten covered in mud from the day's outing. Not just a
little mud, but lots of mud (read about it
here). The initial power-spraying
didn't help, presumably because the York
air compressor was blocking too much of it. Upon limping
home, I removed the compressor, sprayed it off thoroughly again,
and it fired right up. The red stator light on the regulator
came on and the blue stator wire showed 10-12 volts. I guess
I should have shrunk-wrapped those wires like the instructions
told me to. Then again, maybe the alternator itself was full
of mud.
17 Oct 98
- Problem: When lots of electrical stuff is running in the
vehicle (radio, lights, heater fan on high), the check engine
light comes on after a few minutes and indicates insufficient
charging voltage to the battery. The voltage gauge on the dash
reads right around 13.8-14.0 volts. The red stator light on
the regulator turns off several seconds after starting, or doesn't
even come on at all. The voltage on all four wires is correct,
including a stator voltage of 7 V or so on the blue wire.
Solution: Replacing the main regulator with the spare Ford-style
regulator gave all the same voltage readings, but the check engine
light never came on. The spare regulator was replaced with the
main regulator a few minutes later, and then the main regulator
temporarily worked again, complete with red stator light and
everything, but the condition came back. Premier replaced the
regulator under warranty.
late Jan - mid Feb 99
- Problem: Alternator puts out 1.5V (or so) lower on all
wires when engine runs at idle speed. When above 1200 rpm,
all voltages are normal. Alternator emits low-pitched whine/howl.
Welder can't strike an arc, and needs much higher engine rpm to
get to normal welding voltage.
Solution: The stator on the alternator has gone bad. Replace
alternator. Pat had me send it directly to PennTex, who makes
the alternators for Premier.
7-9 Apr 99
- Problem: A broken lower alternator mount (first discovered
Oct '98) finally manged to work
its way loose, and the vibrations cracked the upper mounting
ear on the alternator face plate (the one attached to the good
mount). With the alternator no longer attached to anything,
Bad Things ensued. Fortunately, I was at a stop light just a
few miles from home when it let loose.
Solution: Premier sent me a new face plate for $10. It was
shaped a bit differently than the previous one, and the cooling
fan had to be shimmed out 1-2mm with some washers to clear the
surface of the face plate. Replacing the face plate was a pain,
and in retrospect may have caused the loose battery post mentioned
below. The broken mounting bracket was also replaced from a
Jeep dealer for less than $10.
Summer 1999
- Problem: Alternator often isn't giving sufficient charging
voltate to the battery (diagnostic code 47).
When revving up for welding, sometimes the stator light flickers
out and voltage needle drops. Other times it works, but I must
rev 500 rpm higher to get required voltage (originally, 1800 rpm
would hit the bottom of the red welding range). DC power outlet
can never reach more than 85V regardless of rpm. Voltage at all
four regulator wires looks good.
Solution: At Pat's instruction, sent alternator to PennTex
for diagnosis. They dismantled it & found a little charring
on the back of the stator, as though there had been a short.
A battery post was also loose. They replaced the stator,
brushes, and wiring in the original case, after which it
tested fine for them. S/N when returned was 6989558, p/n
PW170 CRY.
Nov 99 - 31 Jan 2000
- Problem: Partial recurrence of previous problem. Welding
requires a higher engine rpm to achieve same welding voltage
as before. DC power outlet reaches 85V at 1800 rpm, but will
never go higher regardless of rpm. Voltage at all four regulator
wires looks good.
Solution: Doh! The paper label on the voltmeter had gotten
wet and wrinkled, and one of the wrinkles was so tall that it
was blocking the needle from going past 85V. Flattening the
wrinkle fixed the problem. I can still reach the top of the
welding range at 3000 rpm (a comfortable speed for my '95 4-cyl
engine), so I'm not going to worry about the increased rpm
unless it continues to worse.
BTW, PennTex claims the alternator was manufactured in June of '98,
so it's now out of the 12-month warranty period (yet they covered
it in Jan 2000). Premier suggested I send it to Ace Alternators
for repair this time, had it been necessary.
Aug 2000
- Problem: Dash voltage gauge reads 12V. Check engine light
indicates insufficient charging voltage from alternator. No
voltage on orange stator wire at regulator.
Solution: Replacing the normal blue regulator with the
replacement Ford-style regulator got things back to normal.
Despite the regulator being 2.5 yrs old, Premier replaced it
under warranty with a newer, beefier regulator that's basically
one big, chrome, heat sink.
Sep 2001
Contacts are:
- Premier:
Becky Gremillion (secretary? & front-line tech support, Pat's daughter)
Jan Gremillion (office manager, Pat's wife)
Pat Gremillion (head technical dude & master welder)
tech@premierpowerwelder.com
P.O. Box 639
Carbondale, CO 81623
970-963-8875 (tech support & international orders)
800-541-1817 (sales orders)
- PennTex:
Glen Stroud or Dave
7607 Flagstone Dr.
Fort Worth, TX 76118
817-590-2818
- Ace Alternator (authorized PennTex repair station):
Attn: Greg
P.O. 9758
7185 Mohawk Terrace
Yucca Valley, CA 92284
Do you like this site?
Help me keep it going by throwing a few pennies my direction.
Back to Obi-Wan's Popular Mods page
last updated 28 Sep 2001
Obi-Wan (obiwan@jedi.com)
|