Spring-Over-Axle Conversion
on a '95 YJ
Blow-by-Blow
Friday, 9 April
That night after work & dinner, I started tearing into it. I put the
Jeep up on jack stands first. The six 17" stands I borrowed were too
short to get the tires off the ground, so I had to set them on cement
blocks (against David Rush's advice). I also had two 24" stands, so
I put one under each bumper to help stabilize things. I got the rocker
panels 24-3/4" off the ground, which was 5.5" higher than before and
6.5" or so higher than stock. The Jeep really looked tall then, so it
was hard to believe that the SOA lift and new 33" tires would actually
lift the Jeep 2" higher than where it currently sat on the jack stands!
Friday's tear-down consisted of removing the shocks, axle vent hoses,
front track bar, and front driveshaft. I beat on the
pitman arm retaining nut off and on all
night with my new 600 ft-lb Ingersoll-Rand 2131 impact wrench and liberal
amounts of PB Blaster, but it wouldn't budge. I'll try heating it with
a torch tomorrow morning. That impact wrench is already proving its
worth. I'm very glad that I shelled out the $160 to get it
before I did this lift. My low-power air ratchet is also quite handy.
Saturday, 10 April
I got started around 9:30am. I'm really glad I waited to do this
until I got my garage insulated and ready to use. It's cold and windy
this morning with thunderstorms likely. Mark Vogel, a friend who recently
bought his first Jeep ('94 YJ) and is excited to learn all he can, has
volunteered to help me with the heavy stuff. He showed up around 10am.
I put him to work disconnecting the brake lines -- a task which turned
out much more difficult than I originally imagined. I didn't have a flare
nut wrench (3/8" is needed), so we tried using a normal open end wrench.
Two of the five flare nuts unscrewed normally after liberal application
of PB Blaster. A third wouldn't spin on the hard line, but we were able
to unscrew the soft line by rotating it around the flare nut. The upper
end of both front lines were frozen solid, and by the time I finally
broke down and bought a flare nut wrench, the frozen nuts were already
stripped beyond repair. I decided to just cut off the old flare nuts
and re-flare the front lines with a borrowed flare tool.
While Mark disconnected the brakes, I concentrated on removing the
steering pitman arm. As expected, a little heat from a mapp-gas torch
allowed the impact wrench to remove the retaining nut fairly easily.
I then set out to pry the pitman arm off the steering box shaft using
the puller I borrowed from Parts America.
I had doused the arm in PB Blaster quite a bit before starting, but
when I cranked for all I was worth on the puller with an 18" breaker
bar, all I succeeded in doing was breaking one of the jaws off the puller.
Fortunately, I've got a friend that Parts America that swapped me for a
new puller at no charge. I took it home and promptly proceeded to break
it as well, despite excessive use of PB Blaster and a BFH.
I gave up on that for the time being and moved on to unbolting the
axles from the springs before lunch. Just as we were finishing
lunch, Chuque Henry
showed up to help for a few hours. We made use of the extra man
power by pulling the axles and bolting them up under the axles.
Since my new rear spring perches were taller than the old ones (3/4"
vs 3/8", I had to get new, longer U-bolts. The front bolts were
still OK. The front spring retaining plates had to be swapped
left-to-right to keep the sway-bar mounting pins in the right spot.
The center pins that hold the leaf packs had to be reversed since the
perches were now on the bottom. I had hoped to swap my leaf packs
front-to-rear since the rears were sagging a bit more than the front,
but a stubborn spring hanger bolt delayed that til another day.
Getting it out will probably involve destroying the bushing, so I'll
probably wait on that until I upgrade to new poly bushings.
Since my welder was temporarily out of service, we just bolted the
axles in place for the time being. I'll weld the perches in place
later. Technically, my Jeep was now SOA. Too bad we were still a
long way from done.
Sunday, 11 April
We started the day by driving up to Omaha to buy new brake lines.
What to do about new brake lines was probably the biggest question I
had when creating a shopping list for this project. Many places sell
extended brake lines, but most are geared toward 4" lifts. My net lift
(SOA plus my existing add-a-leaves) would be 6-7" over stock, so most
pre-made brake lines would be much too short. I thought about just moving
the hard-to-soft brake line fittings from the top of the frame to the
bottom, thereby requiring shorter soft lines and allowing me to use
relatively cheap, pre-made lines. In retrospect, this is probably what
I should have done, because it would have been much cheaper. However,
I opted to make custom, braided stainless steel lines of the exact length
I wanted using components from Earl's Performance Products
purchased at Sack's Hardware up in Omaha. These components are good,
but they ended up costing nearly double what shorter lines would have.
If I hadn't driven an hour each way to get to Sack's (thinking they'd
be cheaper), I probably wouldn't have bought them. When the dust had
settled, I had spent $152 on new brake lines. My rear line is 26" and
my front lines are each 30", not including the fittings on each end.
I then decided to tear into the Currie slip yoke eliminator kit while
I still had good daylight to work by. The instructions Currie ships
are excellent, and include photos (not just line drawings) for each
step of the way. They do leave out a couple details for which I had
to consult the factory service manual.
- Be sure to drain the case first. Even after draining through
the plug, you'll still get more ATF running out every time you unbolt
a new piece of the case. Have a large-mouth container handy.
- You really don't need to remove the transfer case from the Jeep,
especially if you've already got a significant lift. The biggest
problem with this is that you need at least 9" or so of extensions
to get your socket up to the front output yoke nut. A short-handled
impact wrench works even better, but I had to thread the air hose up
over the tranny. When you remove the yoke, remember to save the little
rubber seal that's shaped like a cross section of the splined output
shaft. At first glance, it looks like a hunk of dried black RTV.
You'll need to put this back on when you reassemble the case.
- When they say you need a "good set of snap ring pliers,"
they don't give a hoot about the quality of the pliers. What they mean
is that you need a set whose jaws can open extremely wide (about 1.25").
The snap rings you'll have to deal with are not the type with holes to
grab onto. They're more like C clips, which means you really want the
kind of pliers that have paddles on the end rather than pins. Battling
these with my small snap ring pliers took more time any anything else,
and eventually proved futile.
[Update: Several years later, I found that Craftsman now makes some
lock ring pliers that are perfect for the job.]
- After unbolting the rear bearing housing from the case,
you should break it loose from the seal by hitting it with a hammer to
rotate it clockwise. Don't hit it straight sideways, and don't use a
screwdriver to pry it away from the case.
- What kind of brain surgeon decided to bolt the NP231 case halves
together with seven 15mm bolts and one 10mm 12-point bolt? 12-point?
Why? Of course, the odd ball is on the very top center of the case, so
your access to it with a box end wrench is quite limited. Once it
came loose, I was able to finish the job with an 11mm, 6-point socket.
- Once you've unbolted the case halves, you still have to pry the
rear half loose from the seal. There are two slots on the edge of the
front half of the case, at about the 10 o'clock and 4 o'clock positions,
into which you can insert a large screwdriver and pry the halves apart.
I found that only the 10 o'clock slot allowed enough clearance for my
screwdriver to pry effectively.
- When the case halves came apart, a 1.5" magnetic washer fell out.
This disk belongs here, in the slot in the
lowest part of the case, just below the front output shaft.
After battling the snap rings for a while with my tiny pliers, I finally
gave up for the night and moved on to the pitman arm, now with my third
pitman arm puller (this time from O'Reilly's, but the same brand puller
that Parts America gave me). Despite warnings about frying the seals in
the steering box, I heated the arm up with my mapp-gas torch, then bathed
it in PB Blaster and beat on it severely with a BFH. Beware -- the
penetrant that runs off the pitman arm will be hot. I didn't
even bother trying the puller at first; I just heated, squirted, and
beat on the arm. While doing this, the tie rod vibrated its way free
of the lower end of the pitman arm and fell to the ground, thereby
eliminating my need for a pickle fork to pry it free. I let it sit for
a few minutes while the penetrant did its thing, then I repeated the
process. After the second iteration, I put the puller on and started
cranking with a 12" socket wrench. I didn't pull to hard since a broken
O'Reilly's puller would have cost me considerably more than the broken
Parts America pullers did. Just when I was about to give up and apply
more heat, I heard a pop. My first reaction was "oh great, there went
my third puller," but when I looked, I found that the pitman arm had
come down 1/8". A few more cranks had it completely off. Even through
leather gloves, the pitman arm was quite hot. I squirted it and the
steering box lightly with water, and both produced steam.
Tuesday, 13 April
Other obligations kept me out of the garage on Monday, but on Tuesday
I found a set of slightly larger snap ring pliers and finished the
SYE kit installation. The new pliers weren't perfect, but they worked
well enough. The rest of the installation went just like Currie said
it would, except:
- I swapped steps 18 and 19 by installing the new output bearing
in the bearing housing before I bolted the housing back onto the t-case.
It seemed much easier this way. A rubber mallet is invaluable for the
latter half of the installation, BTW.
- Currie's instructions don't tell you to re-install the front
output yoke. Be sure to place the rubber gasket back on the end of
the output shaft before you put the nut on. The FSM says to tighten
the nut to 110 ft-lbs. Due to its inaccessibility with a torque wrench,
I just set the impact wrench on setting two and called that good.
- Don't forget to refill the t-case with 3.25 pints of ATF.
[UPDATE: Some time later, I had to replace the oil seal at the
rear output of the SYE kit. The Currie SYE kit uses the same seal
as the stock YJ t-case, which is National (Federal-Mogul) part number
473317. It's 1.687" ID, 2.328" OD, 0.312" deep.]
I also finished torquing down the rest of the suspension to specs and
reconnected the steering. Due to the increased angle of the drag link,
my steering wheel is no longer centered when the wheels point straight
ahead. The drag link length will need to be adjusted to fix that.
When I attempted to reconnect the front track bar with the new extended
bracket from RE, I found that the bolt they shipped was too big to fit
through the holes in the bracket. Looks like somebody grabbed it out
of the wrong bin. 7/16x2.5" should fit better than the 1/2x2" that
they sent me.
I managed to get one of the flare nuts free on the hard brake lines
(on the rear axle) by briefly using the ever-useful torch and PB Blaster.
I can now state from first-hand experience that brake fluid is flammable,
but fortunately not explosive. I didn't want to use the torch on the
front lines for fear of screwing up the paint on the fenders. Clearance
down there is at a premium.
Thursday, 15 April
I got the SS brake lines assembled. The first fitting was a bear,
but they got easier once I got the hang of it. After you include
the length of the fittings (3", something I'd forgotten to consider
when buying the line), the rear line ended up being 29" (13" longer
than stock) and the front lines were 33" (12" longer than stock).
That's great for the rear, since the new T fitting on the axle points
it straight up and the line stays up and out
of the way nicely. The front lines aren't installed yet, but I
have a feeling it'll be a little trickier keeping them away from the
tires at anything less than full droop. On the recommendation of the
guy I bought them from, I got AN-4 fittings. He said AN-3 was only
used for motorcycles and other small stuff, but most of the SS lines
I've seen on other rigs look more like the thinner AN-3 than AN-4.
The AN-4 seems a bit more inflexible than I'd prefer, and it seems a
bit larger than the lines that come with other kits like RE's.
Saturday, 17 April
Well, I can safely say that dealing with the brake lines was by
far the biggest headache of this whole project. I cut off the old,
goobered-up flare nut from one of the front hard lines. Turns out
the flare tool I borrowed only did single flares, so I borrowed one
from Parts America that did double flares. I also found that the
soft line fittings I was sold by Sack's weren't meant for inverted
flare hard lines. I had to run to Speedway Motors and four other
parts stores later on to buy the right fittings.
At least I was able to get the emergency brake cables reconnected.
The passenger side cable was disconnected from it's bracket on the
bottom of the tub and re-routed over the leaves and through one of
the rubber exhaust brackets en route to the bracket on the driver's
side frame rail. The driver's side cable
also goes over the leaves, but otherwise follows the OEM routing
pattern to the frame bracket. This still isn't long enough under
full droop, unfortunately. I only need a few more inches, since the
frame bracket is very near the spring hanger. After several wheeling
trips, I finally drilled a new hole in the bracket about two inches
below the OEM hole. This is about as close as I want to get to the
bottom corner of the bracket. The holes are 9/16", so I had to ream
out a 1/2" hole in order to make the cable fitting fit.
I also managed to lengthen the drag link so my steering wheel is
more or less straight again. Just loosen the clamps at each end
where the rod ends screw on, bathe the threaded portions (including
the slot that the clamp squeezes) with PB Blaster, and start twisting
the middle section of the drag link with vice grips. The front of
the bar must go downward. It'll be a bear at first, but it eventually
gets easier. I needed to turn mine several full revolutions to get
the extra length I needed -- approximately 1/4" at each end.
Tuesday, 20 April
I finished installing the front brake lines last night. I'll bleed
them as soon as help's available. I ended up using vice grips to
break loose the flare nut on the driver's side and then used the same
to reattach it to the new lines rather than cutting and reflaring,
like I did on the passenger side. It was just easier. I still need
to rig up some sort of bracket to secure the mounting point to the
frame, but that shouldn't be too difficult.
I also got the new CV rear driveshaft and installed it last night.
Tom didn't charge me for the D35 yoke U-bolt conversion, for which
he'd quoted me $4 over the phone. The U-bolt conversion was pretty
painless. The threaded holes in the stock yoke are a shade larger
than 3/16". I gradually reamed out the holes using 7/32", 1/4", and
finally 5/16" bits to make room for the larger U-bolt shafts. They
definitely look stronger than those puny little straps that used to
hold the stock driveshaft on. In Tom's words, "Why do they bother
putting eight beefy bolts on the flywheel if they only have those
four tiny screws on the driveshaft yoke?" If you want to do this
swap yourself, Tom says that the U-bolts are Spicer part number
2-94-58X. Be careful not to over-tighten the nuts on these U-bolts.
I pushed one too far and partially stripped it.
Wednesday, 21 April
Chuque came over to help. We started by picking up four of the five
new BFG 33x9.50's from Sam's and having them mounted on my OEM rims.
The fifth tire wasn't in yet -- maybe it had to come from a different
warehouse. Those beasts are much heavier than the 225/75R15
Goodyear Wranglers that came stock. I hope my wife never has a flat
by herself, because she'll never get the bad tire back up on the rack.
When replacing the wheels on the Jeep, we found that the stock scissor
jack is just barely still tall enough to raise a tire off the
ground. My 48" Hi-Lift is plenty tall, but it gets very tipsy
when jacked up that high. The new tires do a better job of filling
the wheel wells, but I think 35x12.50's would look much better in
there. I've still got 8" between the top of my tires and the bottom
of the fender flares and 27" below my rocker panels. The bottom of
the door opening is just shy of crotch level for me (I'm 6'1"); if I
were 2" shorter, I'd be singing soprano after trying to climb out those
first few times. What ever possessed me to put 7" of suspension lift
on a YJ, anyway? I've created a monster. I feel like Dr. Frankenstein --
I had such good intentions when I started, but the project took on a
lift of its own and may now be more than I can handle. I might lose
the add-a-leaf someday. I do like the
70-degree approach angle, though.
Next, we bled the brakes. Remember that brake fluid is very hard on
paint. Every effort should be made to prevent the fluid from getting
on your paint, and that includes remembering to wrench-tighten those
last couple brake fittings that you only finger-tightened the night
before. Once you've cleaned up your mess, resume your
pump-loosen-tighten-release sequence, beginning with the brake farthest
from the master cylinder and working your way closer. When it seemed
that we weren't making much progress with the front right brake, we
jumped ahead to the front left brake and cleared most of the air (there
was plenty of it) out of that line before returning to the right side.
While I haven't ramped it yet, it appears that my front brake lines
are way too long -- a fact Chuque never stopped taunting me for
while helping me bleed the brakes.
By now it was too late & dark to go ramp it, since my PPW alternator
was still in the shop being repaired (that's a tirade for another
day) and I didn't want to run my headlights off just my battery.
I did fire it up and drive it out onto the street beside my house so
I could hose off all the brake fluid we spilled. With no track bars,
sway bar, or shocks, the Jeep was quite tipsy. I still have 3-4" between
my hard top and my garage door, so I still have use of the garage.
While pulling up to the curb, I heard a loud noise and the Jeep suddenly
lurched to the left. Further inspection revealed that I hadn't quite
torqued down the U-bolts around the front springs, and so my front axle
had spun loose and the pinion had climbed to about 45 degrees. Fortunately,
the front driveshaft wasn't attached yet, so no damage was done. It felt
good to finally drive it again after 12 days, even if it was for just 50
feet.
Thursday, 22 April
We tried to go ramp the Jeep during daylight. Just out of the driveway,
the front axle went pinion-up on me. That's twice that's happened due
to the force of turning while slowly accelerating. We straightened it
out, then started to pull back into the driveway and ramp it on a sturdy
plank that was resting in the back of Chuque's D90 (love that 1-ton load
capacity). As soon as I hit the ramp, the extra torque twisted the rear
axle pinion-up. I've decided that it's impossible to torque those U-bolts
down enough to hold the axle in place under any kind of load. Before you
go out on the street, you need to at least tack weld the perches in place.
If you later decide you don't like the pinion angle, grind off the weld
and reposition them.
The rear U-bolts I got were much too long to get a deep-well socket on
the nuts (7.5" tip-to-bend), so I spent the rest of the relatively-short
evening shortening them an inch. I swear, those things must be made of
hardened steel. I went through a couple hack saw blades, an ounce or so
of cutting oil, and a noticeable chunk of my grinding wheel just cutting
eight bolt ends.
Saturday, 24 April
I planned to weld the spring perches onto the axles today so I could
finally ramp it. Numerous friends and one stranger stopped by to talk
for a while, so I only managed to get the front axle done. Correctly
positioning the perches side-to-side along the axle was the hard part.
I must have eye-balled, measured, and re-adjusted things over a dozen
times before I was happy. I ended up dropping the rear pinion about
0.5 - 1 degree below stock to get just a hair more caster. Six months
later, I've seen no problems. My post-lift wheel alignment showed
that the caster was now set at 6.86 degrees on the left and 6.89 degrees
on the right. The acceptible range for a manual tranny is 5.25-7.25
degrees.
I also found out that I can't stick weld worth a crap. The fact that
I couldn't get my face anywhere near the perches while wearing my
welding helmet and therefore did most of the welding one-handed didn't
help any. I eventually got a number of large tack welds that look
like they should hold the perch in place. When welding the axle,
it's very important to just weld a little at a time and cool the axle
tube off with few squirts of water in between welds. If you weld for
too long, you'll boil your gear oil and toast your seals.
Sunday, 25 April
I had a boat-load of stuff to do today, so I got up ridiculously early
and was in the garage by 7am. I got the rear perches welded in place
with about the same difficulty as the fronts. I think I finished around
11am. Note: it's very difficult for one person to slide an axle sideways
while it's weight (though not the vehicle's) is resting on two tires.
After much measuring and adjusting, I finally got the perches setup so
the pinion was about two degrees below the driveshaft angle. On the
test drive, I felt a slight vibration when braking, probably because
the pinion was being forced down (and outside the 3-degree optimum
window).
The track bar relocation bracket that I got from Rubicon Express wasn't
quite right for a lift as big as mine (and probably not for their own
SOA kit, I'd imagine). The track bar is shorter horizontally now, so the
bracket mounting hole needed to be farther to the left than it was.
I ended up grinding a bit off the side of the lower lip of the bracket
so it would bolt to the OEM bracket at an angle. This allowed it to
reach the track bar, and appears to have cured most of the bump steer
that I got when driving without the track bar. I never imagined it
would be so bad without the track bar, and will never consider
driving faster than 10 mph without it again.
Once everything was in place, I headed out for an extended test drive
on back streets. It bounces pretty good without shocks, so I tried
to keep it below 25 mph. Other than that, it's not bad. I finally
got to ramp it on a 50-degree retaining wall at a nearby parking
lot. As expected, my brake lines and vent hoses are
way longer than necessary.
I could easily chop 4" off them and still be
OK. If I'd remembered to include the 3" worth of fittings when
measuring for new brake lines, I'd have probably come out OK. The
driver's side emergency-brake cable is way too short. I'm
losing up to an inch of travel on that wheel due to it. I'm going to
try rerouting it a little, but I may have to replace it with an XJ
cable or something before I go wheeling. While I didn't try it, I'm
sure that disconnecting the front track bar would increase the
articulation noticeably. The rear track bar was removed years ago,
and had a similar effect.
Although the tires look too small for the lift when the Jeep is sitting
in the driveway, that changes under full articulation. The rear tires
do indeed stuff up inside the fender flares. I've still got room for
2" taller tires (35's) before I hit the fore and aft body panels inside
the wheel well, assuming the tires are no wider than 10.5". To go wider
than 10.5", I'd have to drop down to 31" tall tires to avoid trimming
the front of the rear fender flare.
With the front wheels pointed straight ahead, I've still got gobs of
clearance, even under full compression. I could probably fit 35"
tires without rubbing. With the wheels turned at full lock, I'm
already rubbing the springs. The noise of those big lugs clipping
the springs really freaked me out until I realized what it was. Time
to open up the steering stops, I guess. FYI, these tires are mounted on
OEM 15x7 wheels with the stock 5.25" backspacing. A couple years later,
I installed new wheels with 3.75" backspacing,
which fixed the problem with room to spare.
Thursday, 29 April
I finally ordered the shocks on Monday. Calls to several mail-order
places and Rancho tech support determined that I needed 9012's up front
and 9126's in the rear. 9126's are the same length as 9112's, but are
supposedly valved lighter and therefore better for a lightweight vehicle.
I used this
Rancho 5000/9000 shock guide to choose my models, and the shops confirmed
that no more appropriate models had come out since that list was posted.
Since delivery time was most important, I found myself shopping for
3-day shipping prices. Of the several places I called, only a couple
had my models in stock, and of those,
4 Wheel Parts Wholesalers had the best price. Total with 3-day UPS
shipping was $218.08.
They arrived on Thursday as expected (a refreshing change from the rest
of this project) and I set about installing them that evening. First,
I had to make new upper mounts for the front shocks. The pin-style
mounts that the OEM shocks use are uncommon enough that Rancho doesn't
make very many models like that. The 9012's were the only Rancho shock
that was even close to long enough, and it used eyes at both ends.
Rubicon Express makes
shock adapters, but I'm cheap and decided to make my own. A friend
had grabbed me a length of 2" square tube with a 1/8" wall a while
earlier. I simply cut two 2" long sections (1.5" would have worked
better) and then cut off one side of the square to form a U. A 1/2" hole
was drilled in each side of the U for a bolt to mount the shock and in
the base of the U to mount the adapter to the existing shock mount.
The shocks came with a handful of bushing sleeves of various sizes.
After mounting the bottom of the shock, the best remaining sleeve required
an M12x60mm (12mm diameter x 2.25" long) center bolt.
While the brackets sound simple enough to make, they actually took
several hours and were more trouble than I expected. If I'd been
thinking when I put in the rest of my RE order, I probably would have
bought their weld-on mounts for $10/pair and just bought the rest of
the bolts at the hardware store. It's not worth the shipping costs
to get just the mounts by themselves, though. You can read about
my other shock mount modifications here.
If you have questions about SOA or want to discuss it further with other
folks, be sure to check out the
Jeep Tech forum
on our message board.
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Back to Obi-Wan's SOA page
last updated 4 May 2005
Obi-Wan (obiwan@jedi.com)
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